industrial
We know Industrial
Let us demonstrate with this case study.
Client
- Major processing facility in Western Australia
- Annual throughput of 12,000 BCM
- Low-grade feed – highly variable metallurgy
Issues
- High unit and manpower costs
- FIFO logistics and accommodation needing significant upgrade
- Need to improve output, plant availability, safe work and reliability
Key Methodology
- McKinsey’s 7S theory extended with our own 7P methodology
- Documented Work Process flows, Procedures and Protocols
Resolution
- Three-level organisation hierarchy (management, team leaders, team members)
- Shift handovers conducted at workstations
- Reliability Centred Maintenance with planned mini shut downs a key feature of preventative maintenance
- New teams formed: Operator/Maintainers, Maintainer/Logistics Personnel, Technical Planning Support
- ‘Village Council’ formed to administer FIFO facilities
Plant reliability and availability trending at almost 100%
Outcomes benchmarked against similar facilities globally
- Manpower at <50% of that required by competitor facilities
- Costs at <50% of that required by competitor facilities
- Plant reliability and availability trending at almost 100%
- Plant output consistently above guidance
- Safety performance significantly improved – 1st quartile